Filament drive shootout
Inspired by Nophead’s excellent work, I decided to do my own testing. I had the folks up at Najet make me a prototype and pitted it against the existing timing belt pulley from SDP-SI. As with Nophead, I found the worm-gear style pulley to be much superior.

My process was pretty simple. We’re testing the pull strength of the extruder only here, so it involved hooking up the filament drive portion to a force meter (fish scale) and running it until it either stopped or failed. Here’s my setup.
Force Meter
A fish scale 50lbs / 23 kg. I couldn’t figure out how to make it do metric. FAIL! It still worked reliably, and I got a rough sense of what forces were involved. Now that I know my range, I am purchasing a much nicer digital force meter. (Its held down by capa / shapelock… I know, I should really have printed that part)

Filament Harness
Since we’re measuring how hard the extruder pulls on the filament, we need a way to hook up the filament to the force meter. I ended up bolting the filament between two washers and then looping that over the hook. I only rarely had problems after that.

Extruder Drive System
No need for the hot end or anything like that for this test. I laid the electronics to the side. Then I just clamped it to the wood, making sure to clamp in the middle of the dinos and not too hard. The bolts dug into the wood after a bit and made it snap right into place.

Then I just did a bunch of test and measurements. The fish scale did not have a very fast update rate at all (5 seconds?) It also did not have a peak weight or anything like that. I just watched it and tried to remember the highest number. This was a big deal because sometimes the filament itself would either break or elongate and deform. There readings could be slightly low because of that. It was also a bit chilly in the Botcave (its late december
but I’m not going to go that deep on ya.
Here are the results as a google doc:
As for the extruder pulley, yes we will have these eventually. No idea on the timeframe, but having to wait is the price we pay for being as open as possible. I also made the silly mistake of making the diameter of the threaded parts different from the diameter of the current pinch wheel teeth. Its not much of a difference, but I’d like it to be a drop-in replacement. Its a really daunting thing to go into production on a part without a prototype, so it means I’ll probably need to get a new one made. I might have a few other variants made and see how they match up with the results from this one.
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The joy of R&D is that moment when everything comes together and there’s a shiny bit of goodness in front of you, gleaming with potential. This is not one of those stories. 




One of our goals when we started MakerBot and designed the CupCake CNC was to automate one of the most tedious things of all time: frosting cupcakes. This incredibly difficult task has plagued mankind for centuries, but at long last we have found a reliable way to automate the process.
Not only that, but the motorized piston based solution is an inherently flawed approach: The extrusion of a material is based primarily on the pressure, viscosity, and nozzle diameter. There’s not much you can do about viscosity and nozzle diameter, so we’re mucking with pressure. In the motorized piston approach, the pressure builds up gradually as you push the plunger down, and releases as the material either leaves the syringe or you back off the plunger. The result is that you either have extremely slow start/stop times or you have to deal with massive ooze problems.
My first experiment was with some thick, chocolate frosting that you can find in nearly any grocery store. I simply wanted to see if it was possible to use air pressure to extrude frosting, so I wired up a solenoid to a switch and used that solenoid to turn the air pressure on and off to the syringe. I was using a 21GA (0.53mm) needle and a standard 60cc syringe. I hooked it up to the air pressure and opened the valve. Nothing happened right away, but I gradually turned the pressure up until about 50-60 PSI I started getting a frosting extrusion. I kept turning up the pressure to about 80 PSI where I got a really nice, very fast frosting extrusion that was about 0.5mm wide. Success!!!


